Ran the ScAries at Cecil yesterday...here's the full rundown:
1st pass: snapped an axle in the trans. It's pretty nice work if you ask me...I"ll snap a picture of it later. Barry and I swapped in a spare and back out I went
2nd pass: Just wanted to drive the car down the track and make sure the used axle I threw in there was OK. Launched extremely easy, then hit the gas. 19 psi, creeping to 21, shifting easy watching the gauges. Went 12.5 @ 115.8, no spray. All looked well.
3rd pass: Same tune I had set up for GRM, with the exception of a tighter plug gap to hopefully take care of the break up issues I had down there. Went a bit too easy on the launch to where it actually started to bog a bit more than I would have liked, but still managed a 1.72. I was a bit disappointed here because I knew from 20 ft into the run that the track could have taken more. Anyway, the car went:
ST: 1.723
330: 4.76
1/8: time didn't register
1000: 9.215
1/4: 11.010
MPH: 125.12
The car felt great! This was also the same tune I ran in June when it went 11.4's when I was testing the intercooler and found significant pressure drops. Since then, I installed a 3 core cooler and did the divorced downpipe, to get away from the stock swingvalve/downpipe assembly. The difference in how the car felt was amazing. Mid range and top end were huge compared to in the past. It felt downright voilent on shifts. I feel like I'm now really starting to see the benefits of the head work, the intake, the IC and the downpipe. Even though this is on spray, this is still on the Thunderbird turbo, which is a 60 trim T3 that was put into a chrysler .63 housing. It's slightly smaller than a Super 60. :-)
4th pass: After the 11.01, I could taste a 10.9x. I knew that there was more at the line that would likely put me into the 10's, but I started to have some doubts about how much the driveline would take. Other than me, there were quite a few cars that were breaking at the line. The other option was to launch the same and up the boost or nitrous a bit. I debated, but in the end, put a bit more jet into it. I jetted to about 90 hp and went slightly rich on the fuel and took some timing out. At the line, I launched slightly harder and hooked hard again to a 1.66 ST...once again, I think the track would have taken more. The run was absolutely awesome until I missed 3rd gear. At that point, I knew the run was shot but really wanted to watch the gauges and make sure all was well. I put it back into 3rd and let it go. EGT's were around 1500-1550, A/F was 11.2-11.3, boost was 25 psi. Everything looked good. Went to 4th, all readings looked the same. Then, before the 1000 foot mark, I was greeted with a massive spray of coolant from between the nose and the hood and let out, rolling through the traps at 11.35 @ 116.9. Lost the headgasket in #4 at the front of the block. I can actually see the piece missing.
At that point, I decided to call it a day. There was a bunch of TM guys offering to do a quick swap, but I am a bit concerned about other damage in there (this thing is still a non common block, cast cranked, T-II rod/cast piston motor) and would rather get a good look at everything before slamming it back together. I'm a bit worried about that piston. Hopefully the head gasket fuse worked and saved the shortblock.
So close...but next year is right around the corner.