Finally got my hybrid conversion running and driving. I can't control the boost. I even removed the wastegate actuator arm to let the puck float and at 4500 it starts at 15psi and climbing. With the actator connected it spiked to 30psi before blowing off an ic hose. I ran the same turbo in 2006 on an 8v setup and no problems. Its a Garrett gt2871r turbo with a gt3071 compressor wheel and housing, hot side is a ATP.63ar t3 inlet with a 3"id ATP ultimate internal wastegate and 3" mandrel downpipe. 100% stainless header I made and full3" exhaust straight thru muffler. My theory is that there is not enough backpressure in the turbine housing to allow the exhaust to bypass the turbine. Any thoughts? Ideas? I am going to try to machine the wastegate exit on the scroll at more of an angle, try to almost guide the exhaust a little towards the wastegate. Right now its just a hole drilled in the scroll at 90 degrees with exhaust flow, unless the scroll is under pressure, it can't escape out the wastegate. Did I make any sense?
Coy