I don't understand WTH is going on. Line pressure is cranked using a 727 HD spring out of a shift kit, I started using the hollow valve and turbo spring, would shift at 6800 rpm. Changed to the TBI spring and 6500 rpm. I went in and ground some material off the big valve-no change. Last night completely hollowed out the holey valve-it only goes down aprox 1/2-3/4 inside, and then ground out the disc area. You can definately feel its lighter over the stocker. Went for a road test, no difference-WTF???????????? I can't drag race when it shifts this high. I want to go back out tonight but not if I can't get my WOT shift down.