I know this long, but I want to account for as many details as I can and be fair to myself and Wallace. I am trying my best to write this from an unbiased point of view. My intention is not to create waves, but to give an honest accounting of the events that have transpired over the past few months.
I began searching for someone to port the cylinder head for my CSX back in November. I talked to a few guys and then decided to go with Wallace at LWP because he had some seriously impressive numbers. I wasnt looking to spend a huge amount but I had a decent chunk to plop down. Due to my budget constraints I decided to go with a large port, stock valve 782 head. Wallace told me via PM that he had just done one and got 191 (at .400" intake) and low 160's (at .400 ex.). He quoted a price of 800 plus a core and shipping. So, I sent him my core.
He was finished with the job in early January and told me that he was able to get 192/176 (@ .500" lift). He also ran into some trouble with the valve job disrupting the flow numbers, but in order to get the flow back he had all new valves and seats installed at no charge. I was really happy! I promptly paid the bill on January 9th.
The head came with a flow sheet. LWP's numbers on the flow sheet given to me with the head are as follows:
Intake
.100 - 64.3
.200 - 121.7
.300 - 167.2
.400 - 186.6
.500 - 192.2
Ex
.100 - 55.3
.200 - 98.7
.300 - 129.5
.400 - 156.7
.500 - 176.2
When I received the head I took it out and looked it over quickly noticing the nice polish on combustion chambers and epoxy on two intake ports. I put it back in the box and it sat until my cometic head gasket arrived from Cindy a week or two later. I took it out and was getting ready to install it when I began to take a little closer look. I ran my fingers down the short side radius of an exhaust port and noticed a large gouge. I popped a valve and noticed that their were pretty big gouges from the cutting tool along the back side of the bowl. I thought it was strange that it wasnt ground smooth and polished. But, I dont claim to be an expert in anything of this nature so I sent the head over to my machinist to have a look. I told him I would like it flowed. So, I left the head with him to have it flowed. A few days later my machinist's father passed away and he wasnt able to get to the head for another two weeks or so.
This brings us up to last week. I received a phone call from my machinist and he said there was a large descrepancy between the LWP numbers and the numbers from his bench. I told him that I wanted him to flow it in front of me. So, I went over to the shop and he did. While I was at his shop, he further commented that he was appalled at the work that was done on the head, especially the exhaust ports. The numbers he got from his Superflow 600 (converted to28") were as follows:
Intake
.100 - 50.6
.200 - 101.1
.300 - 137.3
.400 - 159.6
.500 - 168.9
Ex.
.100 - 47.5
.200 - 79.3
.300 - 97.4
.400 - 110.0
.500 - 122.0
Of course, I called Wallace. We discussed the issue for a while on the phone. We also exchanged numerous PM's. He explained to me that the gouges were low pressure dibits and the ones in the bowl were special channels. He also explained to me that my machinist's bench was most likely in error.
I told him that I wouldn't feel comfortable sending the head unless he was able to give me refund. Wallace agreed to grant a refund of the amount that I paid him (800 dollars) if I sent him the head.
I would also like to ask Wallace to consider reimbursing me for the core, shipping, and flow bench time should the head be evaluated as inconsistant with the flow sheet he provided. This totals 250 dollars.